The drive gear was heated up to a good 300 degrees on the woodburner, while I blocked up the pulley on the press. Due to tips from an older Two Cylinder Mag, I supported the CENTER of the pulley, as the forces can break the pulley if you just let it set on the rim.
I got the gear down to the shed and started pressing, the gear moved on....but I quickly ran into a problem....I was stupid and used a block of wood against the pulley, and the rim of the pulley began to dig into the wood instead of pressing the gear on.

Dee You Emm DUMB
I had to rearrange the "blocking" and get rid of the wood. Of course this allowed the gear to cool and not press very well at all. I got out the torch and carefully heated up the gear the best I could (not glowing or anything, just trying to heat it) Did that, and was able to press the gear on, though it was pushing the 20 ton cylinder to it's limits towards the end!

The gear/pulley in the press

Up against the snap ring. This snap ring was a ROYAL pain to find, as my original had been torched, and it's not a "standard" thickness, but I finally got one from a salvage yard.

The new gear is ON
After that, I assembled all the clutch linkages, toggles, dog bones, and the roller bearings, etc. I still used my old parts, as they acted fine, and I CAN get to them, if necessary, later. Everything was packed with lots of sticky high temp grease.
After the pulley was assembled, I began the adventure of putting on the first reduction gear cover. I KNEW this was going to be a pain, and I was right. I honestly had no idea how I managed to get it OFF in the first place! It's a big heavy hunk of cast iron, I had prepainted it, and had the gasket precemented to it....which in hindsight was a mistake.
The cover is big and heavy, which is bad enough, but it has to be handled around the crankshaft, the first reduction gear, the hydrualic lines, AND the fact that the cover doesn't go just AROUND the big reduction gear...it goes partially BEHIND it...due to the placement of oil fillers (meaning a portion is smaller than the gear it fits over). Well, you can't bend the cover over the gear, and you can't bend the gear

It takes a whole lot of finagling, and a whole lot of cussing, especially when someone RIPS the gasket trying to go around the gear that can't be moved.
I was going to attempt to make another gasket out of posterboard, but the board from the store was an INCH too short. So I gooped up the gasket I had....luckily it was not ripped in a leak prone area....at the top, and at one of the oil filler holes. THIS time I cemented it to the main case, like I should have the first time, then fought the cover for a good half hour at the last time. I had the hydraulic lines wedged "up" as far as I could go, and fought with different angles 'til the cover managed to bend around everything. Once again, I'm still not sure how. Tightened up all the bolts (of about three different lengths in places)
Then, since my back needed a break very badly, I reinstalled the first gear cover. I had done this once before, but redid it. The first time, I made the gasket...but my paper wasn't large enough and had to split it. I got larger paper and did it again with one gasket.

The first gear cover
I also repainted a few areas that are hidden by the flywheel. They hadn't been painted at the factory, and had some grease there as well.

I should note that the crankcase cover is back on as well, with a homemade gasket as well, since my NOS set had shrunk BADLY, and the cork didn't take well to "stretching". I had that problem a lot with this set of gaskets. Well, I got what I paid for.

I also have new bolts and crudely homemade lockplates in the crank oil slinger. I had loosened it to check the left main clearance a while before...but couldn't remove it due to use of silicone. It was severely glued on!. The original lockplates were falling apart so I took some scrap steel and made them....WAY too thick, and very hacked up looking, but it should work.